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Wednesday, November 1 2017

Today, we modified the drive for our robot as well as cleaned our cart. All extra metal and gears we did not use in our box was removed. In addition we changed our drive so it is now controlled by the digital ports instead of motor controllers. We've been having a problem with the robot losing it's mobility after extended use in the ring. It may be a problem with low torque or traction.


 
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Earth flat
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About Me

The earth is flat

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